This ’68 came into our shop this week with some driveability concerns; and after some sorting out we concluded a switch to a better Holley 4bbl carb to replace the malfunctioning Demon double pumper was the best option and the customer agreed. Car runs substantially better now.
Last week we had a ’99 Cobra brought in that had a Vortech supercharger installed. There was a notable leak at the supercharger; and the car hadn’t been tuned properly. We sublet the rebuild off to Vortech; and upon its return we will be tuning the Cobra here on our dyno.
Customer brought in an ’03 Cobra complaining of backlash noise; disassembling the rear end showed the shims were worn creating a side to side slop as well as the backlash that was the original concern. Now rebuilding entire diff.
When this neat old Ford came into the shop sputtering and coughing; the owner had no idea where to begin or if we could remedy it. Turns out the tired old carb was just in need of a minor overhaul and some adjustments. Runs and drives great now and even picked up a few HP […]
Customer brought in an ’03 Cobra complaining of backlash noise; disassembling the rear end showed the shims were worn creating a side to side slop as well as the backlash that was the original concern. Now rebuilding entire diff.